Example of a real project
Initial situation:Long rotary kiln with a high thermal energy consumption, a O
2 content at ESP outlet of 8 ÷ 10%, very frequent CO peaks
Audit findings: Uncontrolled entries of false air and dilution air at different locations
Erratic solid fuel dosing
No regulation between secondary air fan and fan at stack
Improvements: Removal of false air entries
Installation of a quenching system in front of the ESP
Change of solid fuel dosing
Regulation between secondary air fan and exhaust fan
Results:Thermal energy consumption ↓
Electrical energy consumption ↓